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I thought I'd never have to write this kind of thread, my 02 has been bullet-broof from ownership w/ 2k miles to now w/ 17k and I love this bike.
I recently did a lot of work on her, swapping lots of parts, mostly plastic from a minor crash, but also did some other small mods. The bike has SATO banzai's & PCIII w/ Sato map, flapper mod and ran flawlessly up until the crash. Here is a simple time line, hoping someone more experienced or maybe a new set of eyes can suggest a potential problem.
Oct 09- minor 20mph crash to front end, flipped over & landed on right side, cracked upper cowl, cracked air duct, bent rear stay, snapped aluminum weight in throtttle side handle-bar, snapped right footpeg & brake, minor scratches etc.
Winter-pulled all parts, almost full tank of gas but did NOT stabilize fuel or remove battery, bike sat for 8 months...i know bad bad!
July/Aug-began replacing plastic, small parts etc., battery was almost at 12V(1yr old), hardly needed charging so tried starting bike, full choke & turned over easily but didn't fire, tried several times but no joy, removed plugs & gently cleaned them (torqued right?) still no joy, twisted throttle 1/4 turn and fired up immediately, idled fine and got up to temp fine.
Finished swapping out rear stay, replaced old undertail with OEM fender and most plugs & PCIII did NOT need disconnecting, re-attached everything without any problems. With a new OEM air duct I completely removed the flapper valve per the ROGUE mod directions, but instead of replacing the diaphragm, I cut off the bottom rod flush. Removed the solenoid valve, connector, and vacuum tank and plugged the only remaining vacuum hose. Had to remove Sato cans of course and cleaned off old rtv sealant between pipes, loosened mid-pipes too, to allow for easier line up of pipes, cans and brackets. Re applied rtv between mid-pipe & cans but probably didn't let it set the required 10min. Started bike easily, no problems except a higher than norm idle (1500), took out for short test ride, seemed fine, exhaust note was louder than I remembered but normal, on return, idle was still high but didn't alter. Next day rode bike 30 miles on hwy, temps were avg. 190-200, but exhaust at higher rpms sounded burbled and slight loss of power, got into Boston traffic, temps climbed to 220-224, normal for mine, but still idle @ 1500! In 1st & 2nd gear @ low rpms, seemed fine. On way home, same thing, cruising at 70-80mph in 6th as I rolled on the throttle, burbling sound and loss of power.
Any ideas or suggestions would be greatly appreciated! :notworthy
I recently did a lot of work on her, swapping lots of parts, mostly plastic from a minor crash, but also did some other small mods. The bike has SATO banzai's & PCIII w/ Sato map, flapper mod and ran flawlessly up until the crash. Here is a simple time line, hoping someone more experienced or maybe a new set of eyes can suggest a potential problem.
Oct 09- minor 20mph crash to front end, flipped over & landed on right side, cracked upper cowl, cracked air duct, bent rear stay, snapped aluminum weight in throtttle side handle-bar, snapped right footpeg & brake, minor scratches etc.
Winter-pulled all parts, almost full tank of gas but did NOT stabilize fuel or remove battery, bike sat for 8 months...i know bad bad!
July/Aug-began replacing plastic, small parts etc., battery was almost at 12V(1yr old), hardly needed charging so tried starting bike, full choke & turned over easily but didn't fire, tried several times but no joy, removed plugs & gently cleaned them (torqued right?) still no joy, twisted throttle 1/4 turn and fired up immediately, idled fine and got up to temp fine.
Finished swapping out rear stay, replaced old undertail with OEM fender and most plugs & PCIII did NOT need disconnecting, re-attached everything without any problems. With a new OEM air duct I completely removed the flapper valve per the ROGUE mod directions, but instead of replacing the diaphragm, I cut off the bottom rod flush. Removed the solenoid valve, connector, and vacuum tank and plugged the only remaining vacuum hose. Had to remove Sato cans of course and cleaned off old rtv sealant between pipes, loosened mid-pipes too, to allow for easier line up of pipes, cans and brackets. Re applied rtv between mid-pipe & cans but probably didn't let it set the required 10min. Started bike easily, no problems except a higher than norm idle (1500), took out for short test ride, seemed fine, exhaust note was louder than I remembered but normal, on return, idle was still high but didn't alter. Next day rode bike 30 miles on hwy, temps were avg. 190-200, but exhaust at higher rpms sounded burbled and slight loss of power, got into Boston traffic, temps climbed to 220-224, normal for mine, but still idle @ 1500! In 1st & 2nd gear @ low rpms, seemed fine. On way home, same thing, cruising at 70-80mph in 6th as I rolled on the throttle, burbling sound and loss of power.
Any ideas or suggestions would be greatly appreciated! :notworthy